Hey guys, haven't posted on OCN in forever, but this random refrigeration mock up made me think of putting it here just for shts and giggles.
So I scrapped this heatpipe cpu cooler out of an old Dell and didn't know what to do with it. I saw someone on the web had cut the pipe tips off and bridged them to make a small air to water heat exchanger for an induction heater project. So that got me thinking...maybe you can guess.

And, of course it just so happened that someone threw out yet another mini fridge.
I'm getting good at this.

The compressor is the smaller of the typical sizes found in these things. It's a 2.5cc displacement with 1.3 FLA. Not too impressive, but I've got a holiday to kill.
I formed the existing condensor tubing into a staggered array to work with a 120mm fan. I have a strong 25W delta made fan scrapped out of a Dell to cool it with.
A spark plug works perfectly as a former.

All assembled and ready to be vac'd down. I put it together with regular silver solder, partly because I want to see if it works for refrigeration and partly so I could build it on my desk with my butane micro torch. I have read some techs on the refrigeration forums have used it with success, so WHT. One plus is nitrogen is not as important, since the joints can be made at lower temperatures where the copper will not oxidize. The downside is risk of contamination with flux. I used flux very sparingly and quite frankly I don't care...it's just a quick mock up with a free no name taiwan compressor.
No new liquid line drier, but I kept the lines pinched off, made the joints quickly, and vac'd down asap...again I don't care, as it's just a fun project. It did hold vacuum, so it's at least sufficient for testing.

So the final result after learning about just how to charge a cap tube system here (good read for beginners)
http://www.supco.com/images/pdfs/Manuals-Instructions/Cap%20Tubing%20Manual.pdf
The other part of the experiment is more testing with R-152a refrigerant which is almost identical to R-134a, but just a bit more efficient and at lower temps. The cap tube is the same as what came from the fridge minus about a foot or so. I have no idea what size it is, but I figured a foot less would raise the evap temp and capacity slightly higher. I used a 50W TEC module frozen to the bottom of the evaporator for a load. At 12V 4.1A, that's 50W right there, plus a 20 deg C temp difference across the module, indicating an additional ~30W being absorbed and transferred by the module into the evap according to the datasheet. Not considering the heat gained into the block of ice that is the rest of the evaporator, as well as not considering the thermal resistance between the module and the copper base that would mean a lower delta T across the TEC, it's probably right around 80W of cooling out of this wimpy little thing! The copper base was running at -9 deg C and the evaporating temp was -35 deg C at 10 psi. The cold side of the TEC was -30 deg C.
Motor current held at 1.3A.

So efficiency increased by ~18% at the same time as a roughly 15 deg drop in evaporating temps (most fridge/freezer compressors are rated at -20 deg C evap). With a bit of cap tube experimenting and sacrificing a few degrees, it could probably get up to 90-100W (actually could probably measure at least that much at the base if I actually insulated the evap). Not bad for a piddly mini fridge compressor and a repurposed Dell heatpipe cooler.

So I scrapped this heatpipe cpu cooler out of an old Dell and didn't know what to do with it. I saw someone on the web had cut the pipe tips off and bridged them to make a small air to water heat exchanger for an induction heater project. So that got me thinking...maybe you can guess.

And, of course it just so happened that someone threw out yet another mini fridge.
I'm getting good at this.
The compressor is the smaller of the typical sizes found in these things. It's a 2.5cc displacement with 1.3 FLA. Not too impressive, but I've got a holiday to kill.
I formed the existing condensor tubing into a staggered array to work with a 120mm fan. I have a strong 25W delta made fan scrapped out of a Dell to cool it with.
A spark plug works perfectly as a former.
All assembled and ready to be vac'd down. I put it together with regular silver solder, partly because I want to see if it works for refrigeration and partly so I could build it on my desk with my butane micro torch. I have read some techs on the refrigeration forums have used it with success, so WHT. One plus is nitrogen is not as important, since the joints can be made at lower temperatures where the copper will not oxidize. The downside is risk of contamination with flux. I used flux very sparingly and quite frankly I don't care...it's just a quick mock up with a free no name taiwan compressor.
No new liquid line drier, but I kept the lines pinched off, made the joints quickly, and vac'd down asap...again I don't care, as it's just a fun project. It did hold vacuum, so it's at least sufficient for testing.So the final result after learning about just how to charge a cap tube system here (good read for beginners)
http://www.supco.com/images/pdfs/Manuals-Instructions/Cap%20Tubing%20Manual.pdf
The other part of the experiment is more testing with R-152a refrigerant which is almost identical to R-134a, but just a bit more efficient and at lower temps. The cap tube is the same as what came from the fridge minus about a foot or so. I have no idea what size it is, but I figured a foot less would raise the evap temp and capacity slightly higher. I used a 50W TEC module frozen to the bottom of the evaporator for a load. At 12V 4.1A, that's 50W right there, plus a 20 deg C temp difference across the module, indicating an additional ~30W being absorbed and transferred by the module into the evap according to the datasheet. Not considering the heat gained into the block of ice that is the rest of the evaporator, as well as not considering the thermal resistance between the module and the copper base that would mean a lower delta T across the TEC, it's probably right around 80W of cooling out of this wimpy little thing! The copper base was running at -9 deg C and the evaporating temp was -35 deg C at 10 psi. The cold side of the TEC was -30 deg C.
Motor current held at 1.3A.So efficiency increased by ~18% at the same time as a roughly 15 deg drop in evaporating temps (most fridge/freezer compressors are rated at -20 deg C evap). With a bit of cap tube experimenting and sacrificing a few degrees, it could probably get up to 90-100W (actually could probably measure at least that much at the base if I actually insulated the evap). Not bad for a piddly mini fridge compressor and a repurposed Dell heatpipe cooler.






